Brief History - Enhancing the Methanol-I Plant Capacity
Originally, this plant was designed to operate on feed gas from an ammonia plant consisting of a gas mixture of 75% hydrogen, 22% carbon dioxide, 1% carbon monoxide and some inerts. The reaction of the methanol in gas rich in CO2 is milder as it produces water along with methanol. The crude methanol concentration is also lower. Water further retards the rate of reaction. The two reactions involved here are:
H2 + CO2 ----> CH3OH + H2O + 9.8 kcal/kgmol
H2 + CO ----> CH3OH + 21.6 kcal/kgmol
Normally, a gas mixture of H2 + CO + CO2 is used in a proportion measured in terms of a “R” value (H2-CO2)/(CO+CO2) equal to 2.0 to get an optimum methanol conversion per pass.
Changes to the process included:
1. A methanol chiller was introduced in the gas cooling circuit at the reactor outlet to reduce the methanol concentration and temperature in the recycle gas which helped to increase the methanol production from 4~5 MTD up to 75 MTD level.
2. Setting up a synthesis gas generation unit (SGGU) to supply CO rich gas from natural gas reformer in February 1998. This gas composition is better for methanol production compared to the rectisol wash gas which is rich in CO2. The synthesis gas and distillation loops were debottlenecked by replacing of some control valves, installation of exchangers, and other modifications. The capacity was boosted to 100 to 120 MTD.
3. Replacement of the refining column trays with high capacity Superfrac™ trays from Kostch Glistch India Ltd in October 2002. This, along with other peripheral modifications, were made to increase distillation capacity to 145 MTD.
4. Replacement of the quench adiabatic methanol convertor to Linde’s Isothermal Reactor and debottlenecking of the distillation loops for higher capacity. The capacity of the plant was increased to 160 MTD in September 2003.
Major advantages of Isothermal Reactor include:
Lower pressure drop in reactor
Less temperature variation
Increased life of catalyst
Narrow band of temperature differences in the reactor catalyst bed
Sustained Production Level throughout the catalyst life due to better conversion
Less by-product formation
Effective heat recovery
Compared to the expected 160 MTD production capacity, the unit has achieved a stable production level of 185~190 MTD.
A flow diagram of the new loop is shown in Figure 2 below. In this article, we’ll focus on this latest dimension added to the plant, highlighting the re-commissioning experiences.
Figure 2: Changes in the Methanol Synthesis and Distillation Loops
Figure 3: Methanol Synthesis and Distillation Loops After Changes
Plant Re-commissioning with the Isothermal Reactor
Following the replacement of the quench reactor with the Isothermal reactor from Linde, the plant was ready for start up. The following details the activities associated with start up after the changes were made.
Basic and Detail Engineering - Design Fundamentals
The original plant was designed by Linde with process licensing from ICI. Linde performed the basic engineering for the loop modification and the detailed engineering for the new Isothermal reactor. Based on the data for the new design conditions, a debottlenecking study on the distillation section was carried out in-house by our Technical Services department. Major pre-fabrication work and in-plant erection of the loops which were to be replaced was completed before the final shutdown of the plant. A shutdown schedule of 11 days was planned.
Outline of the Pre commissioning activities
The piping loops were identified and broken down into various process loops per the P & IDs. The plant was broadly classified into three independent sections: synthesis loop, makeup gas loop, and distillation loop. This helped prioritize tasks such that the synthesis and related loops were made ready first. The loops, which were erected before shutdown, were prepared for commissioning by flushing / blowing. Based on the service, the plans for flushing / blowing were prepared and discussed with the mechanical and instrument groups to streamline the activities. All instruments in the circuit were removed from the lines.
The following procedures were used:
For gas lines: Gasket blowing with plant air was carried out starting from 1.0 barg up to 3.5 barg repeatedly, until there was no rust / dust in the line. This was followed by nitrogen passivation / drying.
For liquid lines: Air blowing followed by water flushing was carried out. This was followed by nitrogen passivation / drying.
For steam lines: Gradual warming of the header before insulation was applied for grease removal and rust flushing through the trap bypass. Then steam blowing at full capacity was carried out for half an hour by diverting the open end at a safe location. The header was allowed to cool. This cycle was repeated again till clear condensate was discharged in the trap bypass.
For Running Machines: There was a pair of process pumps in each service. One pump online and one spare. With the higher capacity, some pumps were replaced for higher capacity. The main crude feed pumps and refining column reflux pumps were replaced. With spare pumps, the plant operation was not interrupted during the pump changes. Each replacement took 12 days and included the modification of the base, pipeline, motor, and other ancillary pieces.
Likewise, four control valves were replaced via proper coordination between the operations and project teams. The prefabricated loops were also washed or blown and then dried with nitrogen. These were kept inert and sealed at their ends until they were to hooked up during the shutdown. This also helped reduce the pre-commissioning time for the plant. The start-up boiler feed water circulation pump was commissioned and stabilized prior to shutdown as soon as the errection of the reactor steam drum system was completed.
Both Methanol-I and SGGU operate independently. It was not necessary to shutdown SGGU for the commissioning of Isothermal reactor in the Methanol-I synthesis loop. The natural gas compressors in the SGGU plant get cooling water from the Methanol-I plant header. Since cooling tower was to be taken offline, temporary arrangements to supply an alternate water source was planned to keep the natural gas compressors in the SGGU running. This was implemented prior to shutdown, avoiding a stoppage of the SGGU plant.
Reactor Catalyst Charging
This was the first reactor of its kind at GNFC with spiral wound coils within the shell.
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The catalyst is to be charged on the shell side, while the cooling medium (boiler feed water) flows in the tubes via thermosiphon. During the startup, the boiler feed water circulation pump maintains the water circulation.
Figure 4: Internal View of the Isothermal Reactor
Figure 5: Top Internal View of the Isothermal Reactor
Two catalyst charging nozzles were used with hoppers and 2 ½” dia flexible hoses for charging the catalyst - SACK WISE under the supervision of Linde. A table was prepared to log the number of bags charged per round and the subsequent dip achieved, which showed the packing uniformity. This proved to be a very successful method of charging with good packing density with less than 20 mm of variation in the final height adjustment. A flat and heavy plumb with strong cotton thread was used for taking the dip.
Approximately equal quantities of 20 kg balls/catalyst were filled in HDPE sacks before the start of loading. About 5.2 m3 alumina balls were filled first in four rounds of sack charging. The catalyst bed was leveled so that the balls were just inside the tube coiled bundle. The first dip of catalyst was taken after charging almost half of the catalyst. Thereafter, while monitoring the height, charging continued to completion over approximately two (2) days.
Commissioning activities
The synthesis loop was made available earlier than the distillation loop (6 ½ days) while the total shutdown period was compressed to 8 days by effective identification of the priority of each job. The effectiveness of the pre-commissioning activities was evident during post-commissioning. There were no plugged strainers, control valves by-passing, nor false signals during or after the startup of the plant. Re-commissioning of the plant was completed in less than 4 days time. While, the distillation section modifications were being completed, the synthesis loop pre-commissioning activities were completed. While the catalyst heat up and reduction was proceeding, crude methanol production was coming online.
Peak production levels for the plant were achieved while testing the plant at different feed gas mixtures. The plant has met all process guarantees. Of particular interest has been an improved yield of methanol due to a higher conversion rate and stable reaction conditions. Less by-product formation has led to a reduction of loading in the distillation section.
From this experience, we see that the plant capacity can be increased by understanding the basic principles of reaction kinetics and unit operations. Through integration of technology and the use of improved catalyst, this little plant had been transformed into a giant producer. Proper planning of critical activities like catalyst charging, pre-commissioning of loops, commissioning and guarantee test runs can ensure success.
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